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Factmaps/FactMapsED50UTM32 (OGCFeatureServer)


ID: 417
OBJECTID: 417
wlbNpdidWellbore: 423
wlbName: 34/4-3
wlbHistory:

General

Exploration well 34/4-3 is located in the Marulk Basin north-northwest of the Snorre Field. It was drilled as the third well on the Gamma Structure and had a wedge structure between the Base Cretaceous Unconformity and the Late Jurassic Unconformity as primary target. Secondary objectives were to penetrate the Brent Equivalent and the Statfjord formation. The well is located on the downthrown side of a NE-SW trending major fault, and the sealing nature of this fault was critical for a closure of the reservoir.

Operations and results

Wildcat well 34/4-3 was spudded with the semi-submersible installation Dyvi Alpha on 16 October 1981 after waiting on location for two weeks due to bad weather. The 26" section was drilled with a 21 1/4" BOP installed but after pulling the riser and the BOP a 26" bit was run in the hole since the underreamer did not perform. Drilling of the 17 1/2" section was delayed by nearly two weeks due to the 18 3/4" BOP not meeting requirements. During drilling of the 12 1/4" section electrical problems on the draw works as well as mud pump breakdowns and high pressures was experienced. Drilling the 8 1/2" section included 4 core runs, killing a water/methane kick at 3555 m, changing leaking seals on riser and two intermediate log runs. TD was reached at 4460 m in Late Triassic sediments. The well was drilled with seawater/bentonite/gel down to 516 m, with gel/gypsum from 512 m to 1019 m, with gypsum/polymer from 1019 m to 2209 m, and with lignosulfonate mud from 2209 m to TD.

A methane gas/water kick occurred at 3550 m when the first Late Jurassic sandstone stringer was entered, giving 21 % total gas. A more continuous Late Jurassic sand was drilled into at 3565 m. Two cores (18 m) were cut in this 27 m thick sandstone sequence. The cores consist of shallow marine laminated shale/silt/sandstone. The sandstone is grey, very fine to fine grained with average porosity 10%
wlbHistoryDateUpdated: 2016-07-06T00:00:00