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General
Well 34/10-32 was the fifth well on the Gullfaks South structure. The main objective was to confirm hydrocarbons in the southern part of the structure, and to get data for update of the structural and geological model of the area. The main target was the Statfjord Formation, where the oil-water contact was expected at 3360 m. Secondary targets were Brent Group sandstones and the Lunde Formation.
Operations and results
Appraisal well 34/10-32 was spudded 9 April 1987 by Smedvig semi-submersible installation West Vision and drilled to TD at 3753 m in the Triassic Lunde Formation. Shallow gas was found in the neighbouring hole, and it was decided to set the 20" casing early. There was one meter of shallow gas in this hole as well, but no problems occurred due to this. At setting depth of 13 3/8" casing at 1982 m in the Lista Formation the casing stuck at approximately 1000 m. After several days of fishing 700 m casing was retrieved, while 300 m dropped to the bottom of the hole. The well was sidetracked with kick-off point at 1323 m and further drilling proceeded without significant problems. The well was drilled with spud mud down to 350 m, with gypsum/polymer mud from 350 m to 2940 m, and with lignosulphonate/lignite mud from 2940 m to TD.
The stratigraphy came in different from
prognosis due to faulting. An 8 m thick Brent Group sequence (Ness Formation) came
in at 3170 m, which was 180 m deeper than prognosed. The section consisted of sandstone/siltstone
and was gas-bearing. The Cook Formation sandstones came in at 3236 m, 207 m
deeper than prognosed, and were water-bearing. The well penetrated a large
fault at 3316 m within the Amundsen Formation so that a large part of the
Amundsen Formation was missing. Because
wlbHistoryDateUpdated: 2016-07-06T00:00:00