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General
Well 2/12-2 S is located just 400 m south-west of the 2/12-1 Freja discovery well. The Freja Discovery (named Mjølner up to 1998) lie in a complex faulted area in the North Sea between the Feda Graben to the west and the Gertrude Graben to the east, just north of the border from Danish sector. The reservoir is very deep, ca 4900 m, and the reservoir pressure is one of the highest on the Norwegian continental shelf. Well 2/12-2 S was designed to drill on segment E in the Freja Discovery. Segment E is separated from segment A by a major fault. It was not known if this fault is sealing or not. The main objective for the well was to test the mapped hydrocarbon in place in a Late Jurassic sand unit west of the 2/12-1 compartment. There was no secondary target level known at the time of planning. The well was designed for further use as an oil producer and/ or for extended/ long term testing. Shallow gas was predicted at 467 m and 534 m.
Operations and results
Well 2/12-2 S was spudded with the
semi-submersible installation Mærsk Jutlander on 15 February 1990 and drilled
to TD at 5757 m (5337 m TVD RKB) in rocks of Triassic age. A total of 73 days
(34%) was counted as lost time in this well. It was drilled deviated from below
the 30" casing shoe, with kick-off at 219 m. Drilling proceeded with only
minor problems down to planned TD for the 17 1/2" section at 2790 m. When
pulling out the string stuck at 2631 m. It was backed off at 2280 m, leaving a
fish in the hole. The well was plugged back and sidetracked from 2102 m.
Drilling commenced to 2800 m where the 13 3/8" casing was set. When
drilling out cement in the top 12 1/4" section the pipe stuck again and
eventually a second fish was left in the hole. A second technical sidetrack was
performed with kick-off between 2602 and 2632 m. A third incident of stuck pipe
occurred at 3585 m, but this time the pipe was freed and drilling could
commence. After setting the 7"
wlbHistoryDateUpdated: 2016-07-06T00:00:00