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General
Well 34/10-33 CR was the last in a cluster well bores drilled to appraise the Gullfaks South discovery beginning with well 34/10-33. Well 34/10-33 CR is the re-entry of well 34/10-33 C, which served as a host well for the long-term production test 34/10-T-33 C. In this test the production logging tools failed and the bottom hole pressure recorders were only partly functioning in the long-term production test. Furthermore, an unexpected increase in GOR occurred during the test, and this could not be interpreted based on the available data. Therefore the programme for the re-entry included a new test from the same perforation interval. A further objective of the re-entry was to retrieve and read two pressure recorders that were left in the well 34/10-33 C after the test production. The mean reservoir pressure should be estimated from these data. After testing the well bore would be permanently abandoned.
Operations and results
Appraisal well 34/10-33C was re-entered with the semi-submersible installation Deepsea Bergen on 24 February 1990.
The pressure recorders were retrieved, but both had failed to work.
No cores were cut and no wire line fluid samples were taken.
After testing the well was permanently abandoned on 27 April 1990 as an oil and gas appraisal well.
Testing
Three drill stem tests were attempted from perforations in the interval 3448 to 3517 m (3347.3 to 3395.4 m TVD MSL).
DST 1 was not initiated due to technical
reasons.
wlbHistoryDateUpdated: 2016-07-06T00:00:00