| ArcGIS REST Services Directory | Login | Get Token |
| Home > services > Factmaps > FactMapsED50UTM32 (OGCFeatureServer) > collections > 254 > items | API Reference |
| JSON |
General
Well 7/11-10 S was designed to drill the 7/11-A structure on the Mime Field, on the eastern margin of the Central Graben. The structure is salt induced and consists of a northern, western, eastern and a southern compartment. Oil is proven in the northern compartment by the 7/11-5 well in the Late Jurassic Ula formation sandstone. The reservoir sandstone was deposited in a shallow marine environment mainly by storm episodes into an approximately 100 km long and 20 km wide "fairway". Shales of the Late Jurassic Farsund- and Mandal formations make up the cap-rock. The well was to be vertical down to 2002 m MSL and then kicked off towards the target with an angle of 33.28 degrees. The primary objective was a long term test production from the oil-bearing Ula formation of Area 1 in the northern compartment. Secondary objective was to improve the geological control, and coring was supposed to give good information about the silica cementation above and below the OWC. Shallow gas was indicated in the interval from 318 m - to 425 m MSL.
Operations and results
Appraisal well 7/11-10 S was spudded with
the semi-submersible installation Transocean 8 on 5 July 1990 and drilled to TD
at 4566 m in the Triassic Smith Bank Formation. No shallow gas of importance,
only background gas, was encountered while drilling. Gumbo problems were
encountered in the upper part of the 17 1/2" hole, but hole conditions
improved after increasing the mud weight. The well was kicked off at 2010 m in
40° direction, and the angle built to 35° at 2610 m. While pulling out, the bit
came out with three cones lost. The string got stuck at 3740 m. Fishing
operation was unsuccessful, and a cement plug was set above the fish. The hole
was kicked off from the cement plug at 3550 m and sidetracked. No severe
problems were experienced in the last part of the hole except from low
penetration rate at times and some tight spots on the bit trips. The top hole
was dr
wlbHistoryDateUpdated: 2016-07-06T00:00:00