| ArcGIS REST Services Directory | Login | Get Token |
| Home > services > Factmaps > FactMapsED50UTM32 (OGCFeatureServer) > collections > 254 > items | API Reference |
| JSON |
General
Exploration well 15/12-11 S was a joint operation of Production Licence 038 and 116. It was drilled in the northwestern area of block 15/12 and north of the Varg Field. Well 15/12-1 nearby to the northwest had shows in the Middle Jurassic Hugin Formation, but this was inconclusive with respect to moveable hydrocarbons. Block 15/12 is structurally located in the junction between the Jµren High to the southeast, the Ling Depression to the east, the Sleipner Terrace towards the north and the Witch Ground Graben to the west. The prospect was defined as a multi-target structure, situated on a rotated fault block. Primary targets were Tertiary sandstones of the Heimdal Formation in a genuine closure, in addition to sandstones of the Middle Jurassic Hugin Formation. Secondary high-risk targets were sandstones of Eocene, Late Jurassic and Triassic age.
Operations and results
Exploration well 15/12-11 S was spudded with the semi-submersible drilling installation "Deepsea Bergen" on 10 April 1997 and drilled to TD at 3597 m (3464 m TVD RKB) in sandstones of the Triassic Skagerrak Formation. The well was drilled with seawater and hi-vis pills down to 407 m and with KCl / polymer / Glycol (ANCO 208) mud from 407 m to TD.
Sandstone was encountered in all of the
possible prospective levels except in the Late Jurassic. The two primary
targets however, were more silt/shale dominated than expected. The upper part
of the Heimdal Formation, penetrated at 2680 m had a lower reservoir quality
than expected. These distal parts of the formation were relatively shaly/silty.
More massive and porous sand of the Heimdal Formation was penetrated deeper,
but too deep with respect to a Maureen Field oil spill. The lower reservoir,
the Hugin Formation was penetrated at 3395 m, and was slightly thicker than
prognosed. The only indications of hydrocarbons observed during drilling of
15/12-11 S were weak shows in the Hegre and Vestland Groups a
wlbHistoryDateUpdated: 2016-07-06T00:00:00