{
  "type" : "Feature",
  "links" : [
    {
      "href" : "https://factmaps.sodir.no/api/rest/services/Factmaps/FactMapsWGS84/OGCFeatureServer/collections/254/items?f=application%2fjson",
      "rel" : "collection",
      "type" : "application/geo+json",
      "title" : "The collection document"
    },
    {
      "href" : "https://factmaps.sodir.no/api/rest/services/Factmaps/FactMapsWGS84/OGCFeatureServer/collections/254/items/207?f=json",
      "rel" : "self",
      "type" : "application/geo+json",
      "title" : "This document as JSON"
    },
    {
      "href" : "https://factmaps.sodir.no/api/rest/services/Factmaps/FactMapsWGS84/OGCFeatureServer/collections/254/items/207?f=text/html",
      "rel" : "alternate",
      "type" : "text/html",
      "title" : "This document as text/html"
    },
    {
      "href" : "https://factmaps.sodir.no/api/rest/services/Factmaps/FactMapsWGS84/OGCFeatureServer/collections/254/items/207?f=application/geo+json",
      "rel" : "alternate",
      "type" : "application/geo+json",
      "title" : "This document as application/geo+json"
    }
  ],
  "LayerId" : 254,
  "LayerName" : "Wellbore - History",
  "id" : "207",
  "properties" : {
    "OBJECTID" : 207,
    "wlbNpdidWellbore" : 212,
    "wlbName" : "34/10-20",
    "wlbHistory" : "\r\n\r\n\u003cp class=MsoBodyText\u003e\u003cb\u003e\u003cspan lang=EN-GB\u003eGeneral\u003c/span\u003e\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp class=MsoBodyText\u003e\u003cspan lang=EN-GB\u003eWell 34/10-20 was the first well drilled\r\non the Gamma structure south of Gullfaks Sør in the northern North Sea. The\r\nprimary objective was the Middle Jurassic Brent Group. Secondary objectives\r\nwere Early Cretaceous sandstones, the Cook Formation and the Statfjord Group.\u003c/span\u003e\u003c/p\u003e\r\n\r\n\u003cp class=MsoBodyText\u003e\u003cb\u003e\u003cspan lang=EN-GB\u003eOperations and results\u003c/span\u003e\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp class=MsoBodyText\u003e\u003cspan lang=EN-GB\u003eWildcat well 34/10-20 was spudded with\r\nthe semi-submersible installation Ross Isle on 23 December 1983 and drilled to\r\nTD at 3747 m in the Early Cretaceous Cromer Knoll Group. The well was plugged\r\nback and abandoned without reaching the targets. Engineering difficulties associated\r\nwith high fluid pressure and low formation integrity was the reason why the\r\nwell had to be abandoned. It was drilled with gel/seawater down to 1053 m, with\r\nKCl/polymer mud from 1053 m to 2990 m, and with lignosulphonate mud from 2990 m\r\nto TD. \u003c/span\u003e\u003c/p\u003e\r\n\r\n\u003cp class=MsoBodyText\u003e\u003cspan lang=EN-GB\u003eThe well was dry. Zones with weak shows,\r\nmostly on claystone cuttings, were recorded from 1860 m to 2050 m in the\r\nRogaland Group. \u003c/span\u003e\u003c/p\u003e\r\n\r\n\u003cp class=MsoBodyText\u003e\u003cspan lang=EN-GB\u003eNo cores were cut and no wire line fluid\r\nsamples were taken.\u003c/span\u003e\u003c/p\u003e\r\n\r\n\u003cp class=MsoBodyText\u003e\u003cspan lang=EN-GB\u003eThe well was permanently abandoned on 23\r\nApril 1984 as a junk well.\u003c/span\u003e\u003c/p\u003e\r\n\r\n\u003cp class=MsoBodyText\u003e\u003cb\u003e\u003cspan lang=EN-GB\u003eTesting\u003c/span\u003e\u003c/b\u003e\u003cspan lang=EN-GB\u003e \u003c/span\u003e\u003c/p\u003e\r\n\r\n\u003cp class=MsoBodyText\u003e\u003cspan lang=EN-GB\u003eNo drill stem test was performed.\u003c/span\u003e\u003c/p\u003e\r\n\r\n\r\n\r\n",
    "wlbHistoryDateUpdated" : "2026-02-24T00:00:00"
  }
}