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    "wlbNpdidWellbore" : 274,
    "wlbName" : "7120/10-1",
    "wlbHistory" : "\r\n\r\n\u003cp\u003e\u003cb\u003eGeneral\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eWildcat well 7120/10-1 is located in the Troms I area in the southwestern part of the Hammerfest Basin, close to the Troms-Finnmark\r\nFault Complex. The main objective of the well was to test the Middle to Early\r\nJurassic sands of the B-prospect located in the south-eastern part of the block\r\n\u003c/p\u003e\r\n\r\n\u003cp\u003e\u003cb\u003eOperations and results\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eThe well was spudded with the\r\nsemi-submersible installation Zapata Ugland on 10 September 1984 and drilled to\r\nTD at 2000 m in the Late Triassic. While drilling the 36&quot; hole a boulder\r\nzone was encountered at 210 m to 248 m, which made it difficult to set the\r\n30&quot; casing. When pressure testing the seal assembly before drilling out of\r\nthe 9 5/8&quot; casing shoe, a leak was found in the well head connector. The\r\nleakage was repaired before drilling of the 8 1/2&quot; hole section. The well\r\nwas drilled using gel/seawater down to 534 m, with bentonite/CMC from 534 m to\r\n1302 m, and with gel/lignosulphonate/seawater from 1302 m to TD.\u003c/p\u003e\r\n\r\n\u003cp\u003eNo hydrocarbons were encountered in the\r\nwell. No potential reservoir sands were present above the Middle Jurassic. In\r\nthe Middle Jurassic to Top Triassic interval a net 200 m of good quality\r\npotential reservoir sandstone was penetrated. \u003c/p\u003e\r\n\r\n\u003cp\u003eOne core was cut in the Middle Jurassic\r\nStø Formation from 1570 m to 1584 m. Twenty-two RFT pressure readings were\r\nobtained from 1570 m to 1589 m, showing a saltwater pressure gradient. A fluid\r\nsample was taken at 1573.9 m. The sample contained mud filtrate without any gas\r\nor any smell or sign of hydrocarbons. \u003c/p\u003e\r\n\r\n\u003cp\u003eThe well was permanently abandoned on 8\r\nSeptember 1984 as a dry hole.\u003c/p\u003e\r\n\r\n\u003cp\u003e\u003cb\u003eTesting\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eNo drill stem test was performed\u003c/p\u003e\r\n\r\n\r\n",
    "wlbHistoryDateUpdated" : "2026-02-24T00:00:00"
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}