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    "wlbName" : "15/8-1",
    "wlbHistory" : "\r\n\r\n\u003cp\u003e\u003cb\u003eGeneral\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eWildcat well 15/8-1 was drilled west of\r\nthe Sleipner field, ca 2 km from the UK border. The well was designed to test\r\npossible hydrocarbon accumulation in the sandstones of middle Jurassic age.\u003c/p\u003e\r\n\r\n\u003cp\u003e\u003cb\u003eOperations and results\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eWildcat well 15/8-1 was spudded with the\r\nsemi-submersible installation Glomar Biscay II on 18 July 1981 and drilled to\r\nTD at 4300 m in the Middle Jurassic Fladen Group. Drilling operations were\r\nperformed without significant problems in the 36&quot;, 26&quot; and 17 1/2&quot;\r\nholes. Pipe stuck in the 12 1/4&quot; hole at 2254 m and several times in the 8\r\n1/2&quot; hole. Miscellaneous technical problems occurred while drilling the\r\n6&quot; hole and a gas kick was at 4265 m while tripping. The well was drilled\r\nwith seawater and gel down to 500 m and with gypsum mud from 500 m to 2890 m.\r\nLignosulphonate was added from 1570 m, and from 2890 m to TD the gypsum mud was\r\ngradually depleted and replaced with a gel/lignosulphonate mud.\u003c/p\u003e\r\n\r\n\u003cp\u003eThe well 15/8-1 proved gas and condensate\r\nin sandstone of Middle Jurassic age. The gas/water contact was indicated at\r\n3698 m from the Formation Multi Tester. Oil shows were recorded from 3065 m to\r\n3075 m in the Hod Formation. Five conventional cores were cut in the interval\r\n3658 m to 3705.5 m in the Hugin Formation. Three samples were attempted taken\r\nduring FMT runs. Due to technical malfunctions only 1 sample (from 3668 m) was\r\nobtained.\u003c/p\u003e\r\n\r\n\u003cp\u003eThe well was permanently abandoned on 7\r\nJanuary 1982 as a gas/condensate discovery.\u003c/p\u003e\r\n\r\n\u003cp\u003e\u003cb\u003eTesting\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eOne drill stem test was performed in the\r\nSleipner formation and three in the Hugin Formation. The procedure of the tests\r\nwas similar; after initial flow and build up the well was flowed for\r\napproximately 660 min. producing gas/condensate. Test no. 4 was only flowed for\r\n480 minutes. CO2 was produced in all tests, in concentrations ranging from 4%\r\nto 15%, and up to 8 ppm H2S was recorded in DST2. Two sets of PVT samples were\r\ntaken ",
    "wlbHistoryDateUpdated" : "2026-02-24T00:00:00"
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