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    "wlbNpdidWellbore" : 338,
    "wlbName" : "17/11-2",
    "wlbHistory" : "\r\n\r\n\u003cp\u003e\u003cb\u003eGeneral\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eThe prospect lay in the Egersund Basin\r\nWest of Phillips' marginal Bream and Brisling discoveries. Well 17/11-2 was\r\nlocated to penetrate Middle Jurassic/Triassic sands on the west flank of a\r\nNNE-SSW piercement salt wall. A pair of prominent west-dipping growth faults\r\nmarks the western edge of the salt wall. \u003c/p\u003e\r\n\r\n\u003cp\u003eThe well is reference well for the Åsgard\r\nFormation and Ran sandstone units.\u003c/p\u003e\r\n\r\n\u003cp\u003e\u003cb\u003eOperations and results\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eWildcat well 17/11-2 was spudded with the\r\nsemi-submersible installation Chris Chenery on 12 April 1976 and drilled to TD\r\nat 2644 m in the Triassic sediments. The well was drilled without significant\r\nproblems with bentonite/seawater spud mud down to 436 m and with Lime/PAC\r\n(Drispac)/seawater from 436 m to TD.\u003c/p\u003e\r\n\r\n\u003cp\u003eTop chalk was picked at 1323 m. Dipmeter\r\nevidence indicated several faults within the Early Cretaceous sequence, at 2025\r\nm, 2244 m and 2382 m. Apart from minor gas shows while drilling in the Early\r\nCretaceous/Late Jurassic shales, no hydrocarbon indications (shows and logs) were\r\nseen in the well. Dark grey to black carbonaceous Kimmeridgian shales were\r\npenetrated from 2495 m to 2521 m. The top of the target ?Triassic sandstone at\r\n2521 m was marked by a sudden increase in penetration rate and sand grains in\r\nthe cuttings. A total of 35 m net sand with 17 - 30 % porosity was evaluated,\r\nthe thickest single sand unit was 7.5 m. One conventional core was cut from\r\n2532.7m to 2540.4 m. No fluid samples were taken.\u003c/p\u003e\r\n\r\n\u003cp\u003eThe well was permanently abandoned on 24\r\nMarch 1969 as dry hole.\u003c/p\u003e\r\n\r\n\u003cp\u003e\u003cb\u003eTesting\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eNo drill stem test was performed.\u003c/p\u003e\r\n\r\n\r\n\r\n",
    "wlbHistoryDateUpdated" : "2026-02-24T00:00:00"
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