{
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    "wlbNpdidWellbore" : 895,
    "wlbName" : "2/4-1",
    "wlbHistory" : "\r\n\r\n\u003cp\u003e\u003cb\u003eGeneral\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eWildcat well 2/4-1 drilled by Phillips\r\nwas the first well to be drilled in block 2/4 and the thirty-second to be\r\ndrilled on the Norwegian continental shelf altogether without making a\r\ncommercial discovery. The objective of the 2/4-1 well was to test the\r\nhydrocarbon potential of the Tertiary and top Mesozoic.\u003c/p\u003e\r\n\r\n\u003cp\u003e\u003cb\u003eOperations and results\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eWell 2/4-1was spudded with the\r\nsemi-submersible installation Ocean Viking on 21 August 1969 and drilled to TD\r\nat 1662 m in Miocene dolomite\u00A0 (Nordland Group) where it was terminated due to\r\noil kicks and circulation problems. \u003c/p\u003e\r\n\r\n\u003cp\u003eA 200 ml sample of the kick-oil was\r\ncentrifuged from the mud. The probable depth of the sample was reported to be\r\n1646 m to 1661 m. Due to a high content of water and solids still remaining\r\nafter centrifuging, and because the virgin mud itself contained &quot;a small\r\namount of gasoil&quot;, an exact characterisation of the native oil could not\r\nbe made. However, the oil had high viscosity, and true boiling point\r\ndistillation indicated that more than 50% of the oil was a heavy residue with\r\nboiling point above 400 deg C. The oil was also reported to have a\r\n&quot;disagreeable odor of oxidised hydrocarbons&quot;. No cores were cut and\r\nno wire line logs were run.\u003c/p\u003e\r\n\r\n\u003cp\u003eThe well was junked and permanently\r\nabandoned on 16 September 1969 as a well with strong oil shows. The original\r\nwell objectives were not fulfilled, and since the oil kick could indicate a\r\ndiscovery a new well (2/4-2) was initiated two days later at a location ca 1 km\r\nsouth of the 2/4-1 well.\u003c/p\u003e\r\n\r\n\u003cp\u003e\u003cb\u003eTesting\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eNo drill stem test was performed\u003c/p\u003e\r\n\r\n\r\n",
    "wlbHistoryDateUpdated" : "2026-02-24T00:00:00"
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}