{
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      "type" : "application/geo+json",
      "title" : "The collection document"
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      "title" : "This document as JSON"
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  "LayerId" : 254,
  "LayerName" : "Wellbore - History",
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    "wlbNpdidWellbore" : 1062,
    "wlbName" : "2/7-20",
    "wlbHistory" : "\r\n\r\n\u003cp class=MsoBodyText\u003e\u003cb\u003e\u003cspan lang=EN-GB\u003eGeneral\u003c/span\u003e\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp class=MsoBodyText\u003e\u003cspan lang=EN-GB\u003eWell 2/7-20 was drilled on the &quot;South\r\nEldfisk structure&quot;, later called Embla. The 2/7-9 well, drilled in 1973,\r\ntested oil at uneconomic rates from a thick pre-Late ?Jurassic sand sequence on\r\nthis structure. Well 2/7-9 established a 111 m pay section with average\r\nporosity of 13% and 55% oil saturation. A clear OWC was found at 4387 m MSL. Following\r\na 1986 re-evaluation of the test it was concluded that the poor test results\r\nmight have been due to mechanical problems. Subsequently the 2/7-20 well was\r\nspudded to test the previously encountered sandstones. The objectives of the\r\nwell were to test &quot;economic&quot; flow rates from sands on the South\r\nEldfisk structure below the Late Jurassic shales of the Mandal Formation. At\r\nthe time of drilling the cost of a subsea completion had been estimated to be US$\r\n12 million which meant that flow rates in excess of 286 m3 oil/day were\r\nconsidered economic. Well 2/7-20 was placed on a separate and higher fault\r\nblock in the structure than the one drilled by 2/7-9.\u003c/span\u003e\u003c/p\u003e\r\n\r\n\u003cp class=MsoBodyText\u003e\u003cb\u003e\u003cspan lang=EN-GB\u003eOperations and results\u003c/span\u003e\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp class=MsoBodyText\u003e\u003cspan lang=EN-GB\u003eWildcat well 2/7-20 was spudded with the\r\nsemi-submersible installation Dyvi Stena on 15 October 1987. The well was re-spudded\r\nthree times because of collapsed hole problems. After drilling riserless to 608\r\nm the lower part of the hole collapsed after encountering a gas sand that\r\nresulted in the loss of drill pipe. The well was sidetracked at 234 m, and 13\r\n3/8&quot; casing was set above the Eocene at 2439 m. A drilling break was\r\nencountered at 4084 m. After drilling a further 2 m, 100% sands with good shows\r\nwere circulated up. High pressures together with the long section of open hole\r\nnecessitated plugging back and sidetracking immediately below the 13 3/8&quot;\r\ncasing shoe. No logs were run at TD in this hole before plugging back. Drilling\r\nthe sid",
    "wlbHistoryDateUpdated" : "2026-02-24T00:00:00"
  }
}