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  "LayerId" : 254,
  "LayerName" : "Wellbore - History",
  "id" : "899",
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    "wlbNpdidWellbore" : 2455,
    "wlbName" : "33/9-18 A",
    "wlbHistory" : "\u003cb\u003eGeneral\u003c/b\u003e\r\n\r\n\u003cp\u003eWell 33/9-18 A was drilled to a structure\r\nsituated east of the Statfjord Field and south-west of the Tordis Field. The\r\nmain objective of well 33/9-18 A was to test the lithology of a strong seismic\r\namplitude within the same prospect as drilled in well 33/9-18. Well 33/9-18 A\r\nis a sidetrack from well 33/9-18.\u003c/p\u003e\r\n\r\n\u003cb\u003eOperations and results\u003c/b\u003e\r\n\r\n\u003cp\u003eExploration well 33/9-18 A was spudded on\r\n21 December 1994 with the semi-submersible installation Deepsea Bergen and\r\ndrilled from kick-off at 1974 m to TD at 3597 m in the Late Jurassic Draupne\r\nFormation. The 12 1/4&quot; hole section was drilled with KC1/PAC POLYMER and\r\nKCl mud system to prevent bit balling. No shallow gas was recorded.\u003c/p\u003e\r\n\r\n\u003cp\u003eParts of the 12 1/4&quot; section have\r\nanomalous resistivity data. The MWD data records from 3070 m to TD are missing,\r\ndue to washout, lost signal, stuck pipe and MWD tool lost in hole. No wireline\r\nlogging was performed. 1 core was cut in the Draupne Formation the interval\r\n3397-3404.5 m. No fluid samples were collected. Bit balling was observed\r\nseveral times and a lot of pills were pumped to prevent balling, but minor\r\neffects were observed. Dyno-CC-115 (soap) pills showed best results. Drilling\r\nfrom 3145 m to 3397 m had to stop after 49 m due to bad weather. Drilling\r\ncontinued after 7 days stop and the flow rate was increased to maintain a\r\npressure of 280 bar. At TD the actual pressure was nearly 100 bar less than the\r\n&quot;theoretical&quot; pressure. This pressure drop was caused by wash out\r\nbetween two drill collars. Got differential stuck at 3512 m when pulling out of\r\nthe hole. Cut the string at 3382 m to get free. Extra cost related to logistics\r\nis estimated to approximately 3.3 mill. NOK. The well was plugged and abandoned\r\nafter being stuck for 83.5 hrs.\u003c/p\u003e\r\n\r\n\u003cp\u003eThe well has been interpreted to penetrate\r\nlarge slump/slide blocks consisting of the Brent Group, the Dunlin Group and\r\nthe Statfjord Formation which are deposited within the Draupne Formation. The\r\nstrong seismic ",
    "wlbHistoryDateUpdated" : "2026-02-24T00:00:00"
  }
}