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  "LayerName" : "Wellbore - History",
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    "wlbNpdidWellbore" : 2990,
    "wlbName" : "36/7-2",
    "wlbHistory" : "\r\n\u003cp\u003e\u003cb\u003eGeneral\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eWell 36/7-2 was drilled on the Øygarden\r\nFault Complex, ca 14 km west of the outer skerries of Bulandet in Sogn og\r\nFjordane county. The primary target were the Late Jurassic Sognefjord and the Upper Jurassic Fensfjord formations.\u003c/p\u003e\r\n\r\n\u003cp\u003e\u003cb\u003eOperations and results\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eWildcat well 36/7-2 was spudded with the\r\nsemi-submersible installation West Vanguard on 2 September 1997 and drilled to\r\nTD at 1435 m in basement rock. An anchor test was performed after setting the\r\n13 3/8&quot; casing shoe. Anchor no. 2 and 3 failed the test to 180 ton and\r\nslipped at 170 ton. Piggyback anchors were set on anchor no. 2, while main\r\nanchor no. 3 was lost. Fishing for the anchor chain was delayed 47.5 hrs due to\r\nbad weather. The anchor chain was retrieved and the anchor reset with two piggy\r\nbacks. Both anchors then stood a successful test. The well was drilled with\r\nseawater and hi-vis pills down to 591 m and with ANCO 2000 from 591 m to TD.\u003c/p\u003e\r\n\r\n\u003cp\u003eThe well discovered heavily biodegraded\r\noil in the Middle Jurassic deltaic sandstone reservoir of the Fensfjord\r\nFormation. The overlying Sognefjord Formation sands were tight and contained no\r\nhydrocarbons. A 32.5 m oil column was proven from 931.5 to ca 964.0 m. The\r\nexact level of the oil-water contact could not be determined as it was in a\r\nshaley zone. Oil shows on cuttings were recorded from 915 m down to 1045 m. The\r\nreservoir zone of the Fensfjord Formation was divided into two units, from\r\nwhich only the upper had good reservoir properties. \u003c/p\u003e\r\n\r\n\u003cp\u003eNo conventional cores were cut, but 60\r\nsidewall cores were taken from 603 to 1408 m with a recovery of 56 samples. The\r\nMDT tool was run and 23 good pressure points were acquired in addition to a\r\nfluid sample at 934.5 m. \u003c/p\u003e\r\n\r\n\u003cp\u003eThe well was completed on 22 September\r\n1997 as an oil discovery.\u003c/p\u003e\r\n\r\n\u003cp\u003e\u003cb\u003eTesting\u003c/b\u003e\u003c/p\u003e\r\n\r\n\u003cp\u003eNo drill stem test was performed.\u003c/p\u003e\r\n\r\n\r\n\r\n",
    "wlbHistoryDateUpdated" : "2026-02-24T00:00:00"
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}